[1]秦洪岩.提高火驱注气井符合率的方法与实践[J].石油管材与仪器,2018,4(03):82-85.[doi:10.19459/j.cnki.61-1500/te.2018.03.021]
            QIN Hongyan.Method and Practice of Improving Coincidence Rate in Fire Flooding Gas Injection Wells[J].Petroleum Tubular Goods & Instruments,2018,4(03):82-85.[doi:10.19459/j.cnki.61-1500/te.2018.03.021]
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            提高火驱注气井符合率的方法与实践
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            石油管材与仪器[ISSN:2096-0077/CN:61-1500/TE]

            卷:
            4
            期数:
            2018年03期
            页码:
            82-85
            栏目:
            经验交流
            出版日期:
            2018-06-20

            文章信息/Info

            Title:
            Method and Practice of Improving Coincidence Rate in Fire Flooding Gas Injection Wells
            文章编号:
            2096-0077201803-0082-04
            作者:
            秦洪岩
            中国石油辽河油田公司 辽宁 盘锦 124010
            Author(s):
            QIN Hongyan
            PetroChina Liaohe Oilfield Company, Panjin, Liaoning 124010, China
            关键词:
            火驱符合率影响因素措施
            Keywords:
            fire flooding coincidence rate influence factor measure
            分类号:
            TE357
            DOI:
            10.19459/j.cnki.61-1500/te.2018.03.021
            文献标志码:
            A
            摘要:
            针对火驱注气井符合率低影响火驱开发效果的问题,从注气井的日常管理入手对影响注气井合格率的因素进行详细的分析对现有的工艺流程进行了优化对设备配件进行了改进同时建立相应的管理制度措施实施后提高了机组效率实现了稳定的压力流量空气注入提高了注气合格率
            Abstract:
            With view to the problem of low coincidence rate affecting the oilfield development in the fire flooding well, the factors influenced the qualified rate of the steam injection well were analyzed in detail from the viewpoint of the well daily management. The existing technological process was optimized, the equipment parts were improved, and the corresponding management system was also established at the same time. After the implementation of the measures, the unit efficiency was improved, the stable pressure, flow, air injection were achieved, and the steam injection qualified rate was improved.

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            备注/Memo

            备注/Memo:
            第一作者简介秦洪岩男1983年生工程师2007年毕业于东北石油大学石油工程专业现从事火驱采油工艺的研究与管理工作E-mail:[email protected]
            更新日期/Last Update: 2018-06-25
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